Just throwing this in to this thread guys, I copied it out of the other F150 forum i'm on. I have been chasing a light throttle tip in shudder since new., I'm at 7K miles now. In my case I don't think it's the trans, I have done some mode 6 tests over the last few months with forscan and have seen misfires here and there. So I decided to swap my coil packs as I got them all reasonably priced on Rock Auto (DG-584) Also wanted to note that I noticed running premium gas almost eliminated the problem I have found over the last few months......but i'm back to 87 now.
Anyways I did this yesterday and here is my post to the other forum, I still don't have anymore seat time since yesterday but I'm hoping this is a coil issue:
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Alright all, I have finally changed out all my coil packs this AM (it really only took 15min) I put a thin coat of dielectric grease inside the end of the boot on each coil (maybe an inch up the boot inside but not all the way to the spring or contact point on the spark plug)
I made sure to really seat the coils into the motor in an effort to make sure the spring is contacting the spark plug, this brings up a good point/question......I wonder if some of the problems are that the plug is not all the way in contact with the spring inside the boot. From what I can tell it's not the same old school way where it clips on to the spark plug, it appears to just maybe contact the spark plug? Anyways I am wondering if there is loss of connectivity with this setup or not, but either way I pushed the new coils in as far as possible. I also put a thin coat of dielectric grease on the outside of the coil plug in (where the harness plugs in)
I am not convinced that the original coils were completely seated down to the plug considering it seemed to take more effort than others to remove the coils (but that may not be true)
So the good news is, the truck seems to run smoother and the limited 5 mile drive i DID NOT FEEL THE SHUDDER on light pedal tip in. So I will report back, lets hope this helps us out and maybe just a reseat of the coils could help everyone (just speculating)
Also ran my Forscan and I had ZERO Misfires for the drive, so I'm really crossing my fingers. I am and have been running 87 octane now for the last tank full or two.
So all, I guess I'm hoping this has fixed the issue but not getting my hopes up, I'll report back after some more drivetime ASAP!